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Colgan Airlines Flight 3407 NTSB Crash Animation

Below is the NTSB video animation of the loss of control of Colgan Flight 3407 approach at KBUF (Buffalo, NY), on February 12th, 2009.  The video shows the last two minutes of the flight with the accompanying Cockpit Voice Recording (CVR) below.

Excerpts from CVR transcript:

22:15:06.3       HOT-1    flaps five.
22:15:08.1       HOT-2    what?
22:15:08.8       HOT-1    flaps five please.
22:15:13.5       APP        Colgan thirty four zero seven three miles from KLUMP turn left heading two six zero maintain two thousand three hundred
until established localizer. cleared ILS approach runway two three.
22:15:22.2       RDO-2   left two sixty two thousand three hundred ‘til established and cleared ILS two three approach Colgan thirty four zero seven.
22:15:31.7       HOT-1    alright approach is armed.
22:15:32.8       HOT-2    roger.
22:16:04.1       HOT-1    gear down…loc’s alive.
22:16:06.4       APP        Colgan thirty four zero seven contact tower one two zero point five. have a good night.
22:16:11.5       RDO-2   over to tower you do the same thirty four zero seven.
22:16:21.2       HOT-2    gear’s down.
22:16:23.5       HOT-1    flaps fifteen before landing checklist.
22:16:26.6       HOT-2    uhhh.
22:16:37.1       HOT-2    I put the flaps up.
22:16:42.2       HOT-1    [grunt]
22:16:45.8       HOT-2    should the gear up?
22:16:46.8       HOT-1    gear up.
22:16:50.1       CAM       [increase in ambient noise]
22:16:51.9       CAM       [thump]

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Terrafugia Flying Car Video

I think I’ll be the first to buy one. About time, I just have to scrape together $190K+.

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NTSB Concludes Crew Actions and Safety Equipment Saved lives in Hudson Ditching

Washington, DC — In addition to the decisions and actions of the flight crewmembers, overwater safety equipment likely saved lives that might have otherwise been lost to drowning, the NTSB said.

Today the Safety Board met to conclude its 15-month investigation into the January 15, 2009, accident in which a US Airways A320 jetliner bound for Charlotte was ditched into the Hudson River after striking a flock of Canada geese shortly after departing New York’s LaGuardia Airport. All of the 150 passengers and five crewmembers survived.

Investigators said that had the airplane not been equipped with forward slide/rafts, many of the 64 occupants of those rafts would likely have been submerged in the 41-degree Hudson River, potentially causing a phenomenon called “cold shock,” which can lead to drowning in as little as five minutes.

The accident flight had the additional safety equipment available only because the particular aircraft operated that day happened to be certified for extended overwater (EOW) operations even though current FAA regulations did not require the flight from New York to Charlotte to be so equipped.

Good visibility, calm waters, and proximity of passenger ferries, which rescued everyone on flight 1549 within 20 minutes, were other post-accident factors the Safety Board credited with the survival of all aboard the aircraft.

“Once the birds and the airplane collided and the accident became inevitable, so many things went right,” said NTSB Chairman Deborah A.P. Hersman. “This is a great example of the professionalism of the crewmembers, air traffic controllers and emergency responders who all played a role in preserving the safety of everyone aboard.”

The Safety Board said that the probable cause of the accident was the ingestion of large birds into each engine, resulting in an almost total loss of engine power. Contributing to the severity of the fuselage damage and resulting unavailability of the aft slide/rafts, the Board cited the FAA’s inadequate ditching certification standards, lack of industry training on ditching techniques, and the captain’s resulting difficulty maintaining his intended airspeed on final approach due to task saturation resulting from the emergency situation.

The report adopted by the Safety Board today validated the Captain’s decision to ditch into the Hudson River saying that it “provided the highest probability that the accident would be survivable.” Contributing to the survivability of the accident was the crew resource management between the captain and first officer, which allowed them to maintain control of the airplane, increasing the survivability of the impact with the water.

In addressing the hazards that birds pose to aircraft of all sizes, the report noted that most bird strike events occur within 500 feet of the ground while flight 1549 struck geese at 2700 feet. Investigators said that this difference demonstrates that “bird strike hazards to commercial aircraft are not limited to any predictable scenario.”

Concluding that engine screens or changes to design would not be a viable solution to protect against bird ingestion events on commercial jetliners, the Board made it clear that the potential for significant damage from encounters with birds remains a challenge to the aviation community.

As part of its extensive examination into the behavior of the passengers and crewmembers from the time the plane left the gate at LaGuardia to the moment the last person was rescued in the river, the Board noted that since most of the passengers indicated that they had not paid attention to the preflight oral safety briefing, “more creative and effective methods of conveying safety information to passengers” was needed. Survival factors investigators also found that passengers had significant problems in donning the life vests that were stowed under each seat.

The Board made 35 safety recommendations on engine and aircraft certification standards, checklist design, flight crew training, airport wildlife mitigation, cabin safety equipment, and preflight passenger briefings.

“I believe the safety recommendations that have come out of this investigation have an extraordinary origin — a very serious accident in which everyone survived,” said Chairman Hersman. “Even in an accident where everyone survives, there are lessons learned and areas that could use improvement. Our report today takes these lessons learned so that, if our recommendations are implemented, every passenger and crewmember may have the opportunity to benefit from the advances in safety.”

A synopsis of the Board’s report, including the probable cause, conclusions, and recommendations, is available on the NTSB’s website, at http://www.ntsb.gov/Publictn/2010/AAR1003.htm.

The Board’s full report will be available on the website in several weeks.

NTSB Investigating Near Mid-Air Collision Over San Francisco Between 777 and Aeronca

The NTSB has launched an investigation to determine why a commercial jetliner and a small light airplane came within an estimated 300 feet of colliding over San Francisco on Saturday.

Aeronca N9270E Suspected Near Mid-Air

At about 11:15 a.m. PDT on March 27, the crew of United Airlines Flight 889, a B777-222 (N216UA) destined for Beijing, China, carrying 251 passengers and a crew of 17, was cleared to takeoff from San Francisco International Airport (SFO) on runway 28L and climb to an initial altitude of 3,000 feet.

The first officer, who was flying the aircraft, reported that after the landing gear was retracted and the jet was at an altitude of about 1,100 feet, the tower controller reported traffic at his 1 o’clock position. Immediately following the controller’s advisory, the airplane’s traffic collision avoidance system (TCAS) issued an audible alert of “TRAFFIC TRAFFIC.”

The pilots saw a light high wing airplane, an Aeronca 11AC (N9270E), in a hard left turn traveling from their 1 o’clock to 3 o’clock position. The first officer pushed the control column forward to level the airplane. Both crew members reported seeing only the underside of the Aeronca as it passed to within an estimated 200-300 feet of the 777.

TCAS then issued an “ADJUST VERTICAL SPEED” alert, followed by a “DESCEND, DESCEND” alert. The first officer complied and the flight continued to Beijing without further incident.

NTSB investigator Scott Dunham is traveling to San Francisco to begin the investigation.

###

NTSB Media Contact: Peter Knudson
(202) 314-6100
peter.knudson@ntsb.gov

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NTSB asks to monitor pilots’ talk in cockpits

Government investigators are making an unprecedented push to use “black box” voice recordings to routinely monitor pilots’ conversations and make sure cockpit crews are focusing on their jobs.

The move represents the first time that workplace monitoring could extend into the nation’s cockpits and has drawn intense fire from pilots’ unions who say that the plan is intrusive.

Read the rest of the story here

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